Lorenz Meier
f0a4979da6
Merged master into driver_framework
2015-12-01 12:34:02 +01:00
Lorenz Meier
1e99b04d9c
Fixes in simulator interface
2015-12-01 12:32:22 +01:00
Lorenz Meier
ffdf5076dd
PX4 tasks: Add px4_prctl API
2015-12-01 12:05:15 +01:00
Lorenz Meier
b170467a1d
HRT thread: Set thread name
2015-12-01 12:04:53 +01:00
Lorenz Meier
79a030ec50
Work threads: Ensure they have proper names
2015-12-01 12:04:34 +01:00
Lorenz Meier
85079125f4
posix tasks: Add px4_prctl() call
2015-12-01 12:03:21 +01:00
Lorenz Meier
72287aab3f
Main app: set thread name
2015-12-01 12:02:43 +01:00
Lorenz Meier
d5541ee2a7
sdlog2 writer: Use new prctl syntax
2015-12-01 12:01:52 +01:00
Lorenz Meier
58d5fdc853
Simulator: All app names are lowercase!
2015-12-01 12:01:31 +01:00
Lorenz Meier
eb64a6813f
Sim MAVLink: Return correct type, remove very uninformed comment
2015-12-01 12:01:10 +01:00
Lorenz Meier
05d5292641
MAVLink receiver: Set thread name
2015-12-01 11:56:49 +01:00
Lorenz Meier
1feb30fd39
commander: Set process name on all OS
2015-12-01 11:53:59 +01:00
Lorenz Meier
aa36e54c93
VDEV: More active reporting
2015-12-01 11:53:00 +01:00
Lorenz Meier
5126f81aed
Fix corner cases in timing and in handling poll list iteration in VDEV posix
2015-12-01 10:28:49 +01:00
Lorenz Meier
4b319d2fc6
PWM out sim: Fix corner cases in startup and timeout handling
2015-12-01 10:28:24 +01:00
Lorenz Meier
cf17ef4d41
PX4 semaphores: Add excellent debugging output on failure for Mac OS
2015-12-01 10:28:05 +01:00
Lorenz Meier
0c2b6bf9d1
POSIX: Set the thread name for better debugging
2015-12-01 10:27:39 +01:00
David Sidrane
3ce6ee57e4
Set nunmber of UAVCAN interfaces on HW from top level cmake file
2015-11-30 15:44:36 -10:00
Lorenz Meier
1fc774bbf8
Q estimator: Increase phase margin
2015-11-30 10:26:55 +01:00
Lorenz Meier
9ee4760fe0
Barosim: Simplify to a plain loop without reschedules or sub interfaces. Behaves now. The DriverFramework needs closer inspection for busy-running threads.
2015-11-30 00:41:46 +01:00
Lorenz Meier
a9fb11829f
Commander: Fix scheduling so its not running at higher prio than control apps
2015-11-29 18:50:02 +01:00
Lorenz Meier
65002d279f
Commander: Allow setting home position faster
2015-11-29 18:49:58 +01:00
Lorenz Meier
3c26ca99a0
Q estimator: Increase phase margin
2015-11-29 18:45:48 +01:00
Lorenz Meier
ce1b35d024
Q estimator: Fix scope of sensor voting scheme
2015-11-29 18:41:18 +01:00
Lorenz Meier
66e9abc774
SDLOG2: increase stack size as needed
2015-11-29 17:38:48 +01:00
Lorenz Meier
3515e6ae91
INAV: Increase stack size as needed
2015-11-29 17:38:26 +01:00
Lorenz Meier
f99e14144e
Q estimator: Increase stack size as needed
2015-11-29 17:38:08 +01:00
Lorenz Meier
22c7f72a1c
FMUv4 config: Fix periph 3.3V en signal, fix typo on 8266 RST signal
2015-11-29 17:12:26 +01:00
Lorenz Meier
a4aa844151
FMU driver: Slightly increase run interval to save load
2015-11-29 17:06:54 +01:00
Lorenz Meier
00e9804b5a
Mixer: Fix dependencies
2015-11-29 17:05:39 +01:00
Lorenz Meier
94eff8d9a8
Commander: Fix scheduling so its not running at higher prio than control apps
2015-11-29 17:05:01 +01:00
Lorenz Meier
cb286d0ae6
FMUv4: Initialize complete board correctly
2015-11-29 17:03:50 +01:00
Lorenz Meier
57ce3cfd01
FMUv2: Remove unneeded code
2015-11-29 17:03:19 +01:00
Lorenz Meier
f8ccac69bc
FMUv1: Remove unneeded code
2015-11-29 17:03:06 +01:00
Lorenz Meier
fa197ee490
FMU driver: Run slightly faster to accomodate S.BUS
2015-11-29 14:55:25 +01:00
Lorenz Meier
151402748e
S.BUS input: Be less sensitive on timing
2015-11-29 14:55:03 +01:00
Lorenz Meier
c28f394c3c
Gyro sim: Remove unused perf counter
2015-11-29 13:42:42 +01:00
Lorenz Meier
f4f143927f
MPU9K: Remove unused perf counter
2015-11-29 13:41:17 +01:00
Lorenz Meier
44d32a31d1
MPU6K: Remove unused perf counter
2015-11-29 13:41:02 +01:00
Lorenz Meier
05d248480a
Initialize FMU actuator control feedback struct
2015-11-28 11:37:59 +01:00
Lorenz Meier
d07c69d329
MAVLink: Output RC inputs faster
2015-11-28 11:16:21 +01:00
Lorenz Meier
d407f0dfe7
Fixed FMU code style
2015-11-28 09:13:15 +01:00
Lorenz Meier
b196d29662
FMU driver: Output and read at 400 Hz
2015-11-28 09:13:15 +01:00
Lorenz Meier
a3eeafebeb
Enable UART6 and enable S.BUS. Tested to work.
2015-11-28 09:13:15 +01:00
Lorenz Meier
6bc6eda295
Fixed drivers
2015-11-28 09:13:15 +01:00
Lorenz Meier
5500ad16d8
Fix RC
2015-11-28 09:13:15 +01:00
Lorenz Meier
bb2d3a36b7
Remove old build system artifact
2015-11-28 09:13:15 +01:00
Lorenz Meier
05840535f1
Fix math tests
2015-11-28 09:13:15 +01:00
Andrew Tridgell
46631b5c8a
mpu6000: work around apparent ICM20608 bug
...
undocumented register 0x11 sometimes starts with value 0, which gives
an offset on the Y accel axis of 2.7m/s/s. It sometimes boots with
0xc9, which gives a zero offset. Force it to 0xc9 to get consistently
correct behaviour
2015-11-28 09:13:15 +01:00
Lorenz Meier
38724d9e12
Sumd: Fix code style
2015-11-28 09:13:15 +01:00