Daniel Agar
cd7713eba2
boards: delete unused variants
2021-02-22 20:08:36 -05:00
Daniel Agar
414f9f81d9
move fake GPS to standalone module
2021-02-20 14:13:36 -05:00
Daniel Agar
ab0d0fd0be
uORB move to PX4 platform layer
2021-02-17 11:25:56 -05:00
Daniel Agar
44df0fb7a2
Analog Devices ADIS16448 rewrite
...
- new IMU driver structure with state machine (no sleeps in bus thread)
- verify all configured registers and trigger reset on failure
- detect if DIO1 or DIO2 are actually connected for data ready interrupt usage
- don't use CRC-16 on burst transfers except for verified lots
2021-02-16 10:29:07 +01:00
Daniel Agar
fb2a199621
delete unmaintaned mkblctrl driver
2021-02-14 10:38:15 +01:00
Daniel Agar
a257120e8d
boards: use new param default mechanism
2021-02-12 08:27:47 -05:00
Daniel Agar
8f0918a16b
boards: remove unused linker __param section
2021-02-08 23:22:48 -05:00
Daniel Agar
a2442ffb48
board: enable UAVCAN sensors by default on F7/H7
2021-02-02 09:01:12 +01:00
Daniel Agar
f0d1f1d679
boards: disable BDMA on STM32H7 for now
2021-01-28 21:16:23 +01:00
David Sidrane
455f762516
px4_fmu-v6x:Support RC03 HW
2021-01-25 09:18:24 +01:00
Daniel Agar
1ec10bfcc6
boards: disable CONFIG_ARMV7M_LAZYFPU again ( #16573 )
...
- this was causing hard faults on the CUAV Nora and possibly other boards, disabling everywhere until we fully understand the root cause
2021-01-17 22:40:21 -05:00
Beat Küng
26e8c231b0
v5x,v6x: move mtd_caldata after mtd_id partition
...
to avoid losing factory calibration params on existing setups
2021-01-15 10:57:20 -05:00
Beat Küng
9f5dee2ecf
v5x/v6x: update IMU sensors (remove ISM330DLC)
2021-01-12 09:55:59 -05:00
Daniel Agar
cb74cb8692
boards: enable CONFIG_ARMV7M_LAZYFPU everywhere
2021-01-12 09:04:38 +01:00
Daniel Agar
763c3b8fda
boards: start enabling multi-EKF by default on F7/H7
2021-01-10 17:56:34 +01:00
Matthias Grob
7545249215
Add flight_mode_manager to all targets with mc_pos_control
2020-12-30 10:25:08 -05:00
David Sidrane
22bc176885
Added mft for queries
2020-12-02 20:40:23 -05:00
David Sidrane
44ffc855dc
px4_fmu-v6x: Use px4_platform_configure
2020-12-02 20:40:23 -05:00
David Sidrane
ff87bc0fda
fmu-v6x:Bootloader init NULL console
2020-10-28 14:25:25 -04:00
Daniel Agar
233949a377
NuttX upgrade to 10.0.0+ defconfig changes
2020-10-28 14:25:25 -04:00
Beat Küng
274ccaf57c
system: include shutdown lock to BOARD_INDICATE_ARMED_STATE
...
BOARD_INDICATE_ARMED_STATE was only set during arming, so an external
component might have reset the board during param save, leading to param
loss.
This extends the API to trigger the arming state also while the shutdown
lock is taken.
2020-10-09 08:23:47 +02:00
David Sidrane
529d816a39
px4_fmu-v6x:Support ETM Hardware Trace
2020-09-28 10:59:39 -04:00
Tanja Baumann
b5ebdb8e41
add system command to get and set system time
...
* add system_time command for all boards
2020-09-26 13:09:01 -04:00
David Sidrane
c7642288db
px4_fmu-v6x: Updates for NuttX 9.1.0+ External schedule_note
2020-09-16 21:32:04 -04:00
David Sidrane
1a51a84130
px4_fmu-v6x: Updates for NuttX 9.1.0+ External schedule_note
2020-09-16 21:32:04 -04:00
David Sidrane
72c681134d
px4_fmu-v6x:Add support for DMA on SPI6
2020-09-16 21:32:04 -04:00
David Sidrane
f870594f1d
px4_fmu-v6x Updates for NuttX 9.1.0-
...
px4_fmu-v6x: defconfig MMCSD enable multiblock
2020-09-16 21:32:04 -04:00
SalimTerryLi
c037dbef21
Rename and move src/drivers/adc to src/drivers/adc/board_adc
2020-09-07 23:09:20 -04:00
Daniel Agar
2c3441aa90
boards: reduce CONFIG_NFILE_DESCRIPTORS 15 -> 12
...
- reduced now that calibration uses uORB::Subscription
- can likely be reduced further (perhaps < 8) with additional testing
2020-08-21 10:12:13 -04:00
David Sidrane
22a7bf6ec7
px4_fmu-v6x Fix BOARD_TYPE
2020-08-14 11:23:16 -04:00
Daniel Agar
e3d31a881e
boards: NuttX disable posix message queues
2020-07-17 17:00:21 -04:00
David Sidrane
28a695dce4
px4_fmu-v6x:imu/bmi088->imu/bosch/bmi088
2020-06-19 19:13:20 -04:00
Daniel Agar
6f6efd60b7
boards: centralize optional external I2C sensor start
...
- configured with new parameter SENS_EXT_I2C_PRB
2020-06-10 09:04:13 -04:00
David Sidrane
82b87adfb3
px4_fmu-v6x:default phy is LAN8742
2020-06-09 08:14:22 +02:00
Daniel Agar
5e7d2e830d
boards: delete old board.h boilerplate
2020-06-08 19:10:33 -04:00
David Sidrane
73bb18a053
px4_fmu-v6x: Limit Slew rate So IMU works with DMA
...
The defualt in NuttX is OSPEED of 50Mhz. This is realy a slew
rate control. At the default high slew rate the overshoot was
.7 Volts. On a ICM20649 this was causing the device to output
garbage. All 0s
N.B. A passive scope or Logic analyser's probes load will mask
the failure. Useed a FET probe to verify the issue.
2020-06-02 13:02:51 -04:00
David Sidrane
5d90c31632
Added PX4 FmuV6X
2020-06-02 13:02:51 -04:00